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Restoration diary

Reports of restoration work on 50029 and 50030.

Working party report 24th July 2016

​Dave Rolfe and I were on site today. Dave was freeing up one of the cab doors on Repulse while I carried on undercoating in the Thin Man's and over the cubicle inside the same locomotive.  Ian Kemp was on site the previous Saturday and they unbolted the remaining pipes and connections to the radiator fan currently inside 50030,...
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Working party reports May-June 2016

The battery charge diode reinstalled in the electrical cuible inside 50030 after testing and repair.
New volunteer Andy Blofield getting his hands dirty for the first time.
​29th May 2016Dave Rolfe was helping remove usable parts from an old coach which is to be sent for cutting, and he asked for any electrical items he could salvage. He got two small steel cabinets and several lengths of conduit plus various elbows and tees. The smaller of the two cabinets could be useful as a connection box for the severed conduit o...
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Working party reports April-May 2016

Refurbished fire bottles area inside 50030.
​18th April 2016I brought the good battery charge diode back and carried on cleaning and undercoating cubicle covers, scraped loose paint off the roof over the cubicle and finished re-threading the holes for the slotted covers right at the top of the cubicle.Dave Rolfe has cleaned and painted the area behind where the fire bottles stand next to the...
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Working party reports and updates January-April 2016

Battery charge diode ex-50030 (left) and a spare from RRRG stores (right). The ex-loco component gave suspect results during routine testing and both were taken for more in-depth tests courtesy of another group.
​A compilation of work party reports since our last updates.25th January 2016Dave Rolfe and Peter Carter continued to put the new oil into the ex-50008 power unit, I refitted the reverser actuator cylinder and checked out the battery charge diode again, which still gave strange readings, and re-threaded some more of the electrical cubicle cover hol...
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A host of updates coming soon...

Apologies for the radio silence folks.  RRRG hasn't shut down and ceased to exist.  It's more that we've been busy both on group matters and with our own personal lives.  A number of updates should follow later today.
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Work party reports 30th November 2015 and 17th January 2016

Work party reports 30th November 2015 and 17th January 2016
The reverser for 50030 with the air connection temporarily attached to the actuator. We successfully operated the air valves from an off board compressor to prove we had the correct connections.
On 15th November, Ian, Pete and Dave continued filling the power unit with the new oil, checking for leaks along the way, and blanking off pipes that cannot be fitted before the PU is lifted back into Repulse. Dom and I continued belling out the electrical cubicle wiring, and completed all the cables from the compressor, rad fan, ...
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Working party report 25th October 2015

Working party report 25th October 2015
The work party was attended by Dave Rolfe and myself plus Mark Burrows in the morning. Mark dropped off a set of cab desk panels for me to take a look at, then spent the rest of the morning searching through our stores of other cab parts. The panels appear to be in good condition but are missing the speedometer.  We have this item in stock els...
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Working party report 3rd October 2015

Working party report 3rd October 2015
Ian Kemp, Peter Carter and Dave Rolfe fitted two oil filter housings to the power unit,  and cut down a spare to make a further shallow one (which Dave welded up), so they can pump oil round the power unit when we get to that stage. I fitted three cubicle doors I had left to dry last work party, cleaned two large ones and topcoate...
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Working party report 20th September 2015

Ian Kemp, Peter Carter and Dave Rolfe removed pipework in Renown to get at, and remove, the fuel lift pump/alternator, which we need for Repulse, but not before it's been sent away for overhaul. (We often get asked why we don't strip Renown to help restore Repulse; the simple answer is that there isn't much on 50029 that we need for 50...
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Cab restoration update

At the last work party I attended I took home with me a number of items to repair/overhaul or look into replacements.The first items were a pair of air horn valves, two of which are our three spares.  Despite looking rather battered the first one (photo 1) was in generally good condition.  I stripped it down, gave it a good clean, sourced...
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Working party report 6th September 2015

A slightly frustrating day was had.  Ian, Dave and the mechanical team struggled all day to try and fit the last remaining piece of oil pipe to the power unit so they can pump oil round it, but despite cutting more and more off one of those big hardened steel plates holding the supporting sleepers together, they still co...
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Working party reports 26th July and 9th August

Working party reports 26th July and 9th August
Refitted oil (pink) and water (blue) pipes leading to the heat exchanger recently refitted to the 50008 power unit.
The oil filters and strainer were refitted to the power unit recently. The grey caps above the blue water pipe are the tops of the oil filter housing. One of these contains the strainer with the rest being filters.
Dave Rolfe continued to make progress cleaning out the air filtration compartment between the radiator and engine rooms.
The new CU5 radiator fan control unit was test fitted into 50030 and is seen alongside the CU7 ETH field detector unit.
On 26th July Pete and Ian rifled through our extensive spares collection to find pipework needed to refit to the ex-50008 power unit as its rebuild continues. I carried on refurbishing and painting the electrical cubicle doors and framework. I also rediscovered a large quantity of Class 56 electronic units that we had speculatively bought from scra...
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Open Day 21st June 2015

Open Day 21st June 2015

Renown Repulse Restoration Group is holding an Open Day on Sunday 21st June 2015 from 2 PM onwards at our Rowsley South, Peak Rail base.  We hope to attract new volunteers and investment into our project.  All are welcome, whether experienced preservationists or complete beginners!  RRRG members will be on site to show you around 50029 and 50030, as well as discuss our facilities, restoration plans and how you can help as a future volunteer for RRRG.  We look forward to seeing you then and there.  Peak Rail are also hosting a classic bus event on the same day, providing an additional attraction for visitors to the railway.

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Working party report 19th April 2015

Working party report 19th April 2015

During the work party of 19th April Andy Rowlands connected up the reverser air piston coils and tidied up the cables in the electrical cubicle in 50030, then started investigating the severed cables under the main cubicle walkway. They appear to be from the DSD relay box but further investigation will be required to trace them exactly.

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Peter Carter and Ian Kemp together with Dave Rolfe continued fitting oil and water pipes to the ex-50008 power unit (see previous report, Power unit progress) in continued preparation for its use inside the overhauled 50030.

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Work party report 21st September 2014

Work party report 21st September 2014
Dave, Pete and Ian disconnected and removed the four sections of airshaft round the power unit flywheel and bolted up the second intercooler, which Dave then painted. I continued cutting and fitting cubicle air pipes, removed the Z23 resistor and a now-redundant cable from it to the CU6, in preparation for fitting an electronic device in its place as part of the CU6 upgrade.
 
As we were packing up we were greeted by the sound of eight Rolls Royce Merlins as both the preserved airworthy Lancasters flew over Rowsley.
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Spare electrical cubicle progress

Spare electrical cubicle progress

If you have been following RRRG for some time, you will remember that about a year ago we purchased and collected a number of spare electrical parts from the owners of 50021 Rodney.  Amongst these was the electrical cubicle originally in 50011 Centurion before that locomotive was scrapped.  Our reason for purchasing the cubicle was to use as a donor for rebuilding 50029's cubicle; as a rule of thumb the items that were removed from 50030 before we bought the locomotive were carefully unscrewed and the wiring in the electrical cubicle was in good condition.  The same cannot be said for 50029 unfortunately, with many of the cubicle wires having been cut.  To save the headache of pairing loose ends we aim to transplant the relatively intact wiring loom from the ex-Centurion cubicle into 50029.  That there were a good number of other components in the donor cubicle that would be useful for 50029 was a bonus.  The actual frame of the ex-50011 cubicle is however not in such good condition as the cubicle frame already in 50029: many of the catches for the doors are either bent or broken and it is obvious the cubicle has led a hard life since the locomotive it resided in was scrapped.  For this reason we cannot just swap the cubicles around between Renown and Centurion and a process of making one good one from two halves is necessary.

These pictures were taken on 9th June 2013 and show progress on the careful stripping of this cubicle and some of the parts we have recovered from it.  Electrical volunteers Steve Tripp and Andy Rowlands are shown at work but credit must also go to Julie Rollason and Sarah McCall for their invaluable assistance with this sub-project.

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The complexity of the wiring loom is obvious from these pictures which show volunteers Steve Tripp and Andy Rowlands removing some of the last major components before we make a decision on how to tackle the wiring loom.  A good number of useful items have been recovered from this cubicle for re-use in 50029, as shown below.

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Shown below is one of the cubicle doors from the ex-50011 cubicle.  We have already refurbished the equivalent door and installed into 50030 and we have a better example in stock for 50029.  This is actually one of the better condition parts of the cubicle frame and speaks to the state that the ex-50011 electrical cubicle is in.

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The next task is to assess the wiring loom in the 50011 cubicle and how best to remove it.  As the pictures show it is a many-tentacled monster and will require considerable thought as to the best way forward before we dispose of the frame of the 50011 cubicle.  With the size of the "thin man's passage" inside a 50 round the side of the electrical cubicle now not befitting our volunteers' physical profiles, we may also look to lifting the cubicle out of 50029 as a way of proceeding.

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Workparty report for 2nd September 2012

Today I are be mostly...sorry been watching too many episodes of the Fast Show. Dave had spent the week on site as he's still off work following his operation & he's cleaned & painted most of the water & air inlet piping for the ex-008 power unit. Mark B dug out of the stores the two sections of protective shields for the A side generator conduits & cleaned and undercoated them; one each for 29 & 30. He also sorted a third section of the gen conduits, loosened off the joints and began removing years of layers of paint. I and my girlfriend Julie belled out and marked both sets of wiring from the cab AWS sunflowers to the AWS relay box, though removing the lid of the relay box proved difficult as two of the fixing bolt heads had been broken off some time ago, and I had to put an angle-grinder through the one stud to release the lid. I brought away the shaped mounting bracket from No.2 cab and the sunflower dial from No.1 cab to clean the contacts.

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Workparty report 12th August 2012

Ian & Pete cleared various debris out of the sump of the power unit, and started cleaning & painting sections of inlet air piping. Dave...supervised, as he is still recovering from being under the knife for a hernia and is excused duties for the moment. Mark cleaned & sorted another section of conduit for the generators, to go with the two sections he had previously done, so three down, 13 to go. This is not as easy as it sounds, as most of the lengths of conduits had been separated from each other for easier storage, so it was a case of multiple visits inside Repulse & our stores to find the right sections.

I test-fitted one of the new Z70 resistors, and found it fits the existing brackets perfectly. I just need to properly space the tapping bands, then it can be fitted permanently.

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Collecting gas bottles

Gas bottles on trolley

Our gas bottles on the trolley used to collect them; oxygen (black) and acetylene (maroon).

One of those "must get round to doing that sometime" tasks hanging over RRRG has been to collect a couple of cylinders of oxygen and acetylene with which to power our cutting and welding equipment. Although there is a BOC distributor just across the A6 from Peak Rail's Rowsley South site they have limited opening hours which are somewhat inconvenient for the regular on site RRRG volunteers.  Tim and I decided we would head up to Rowsley last Friday night in order to be on site in the morning ready to collect the gas. So, shortly after 4 o'clock on Friday afternoon I hit the road to drive the 170 miles or so from Reading to deepest Derbyshire whilst Tim got a train from Peterborough to Matlock, where I would meet him. I got delayed by the usual Friday traffic whilst Tim got delayed when 66008 decided to investigate the ballast on the Midland main line near Duffield. (I did however make it through Bletchingdon on the A34 without incident after my two year anniversary earlier this month, and once on site, Dave was as helpful and complimentary as ever that my latest car was retaining its factory-fitted styling so well).

The cylinders are now in situ at RRRG headquarters. One of the main uses we will have for them is to heat up some bolts and pins on our spare bogies which are absolutely stuck fast and won't shift any other way.  In particular there are some arms secured by pins and bolts which prevent the traction motors being removed from the bogies and we want to either free these off, or if necessary, cut them off (we have plenty of spares) in order to free the motors for removal to Bowers for overhaul.


Intake manifolds

Aluminium air intake manifolds destined for the ex-50008 power unit. The foreground example awaits the removal by wire brushing of years of dirt and grime to reach the standard of the background pair, which Dave Rolfe described as "Rolls Royce quality"!


Air intake manifolds with red oxide primer

After treatment with the wire brush, Tim and I set about red oxide primer coating of the manifolds we treated that day, as well as returning to some that other RRRG volunteers had already treated, just to ensure that "Rolls Royce finish"!

With the main excitement of the morning over, and after a few steadying cups of tea and brunch at the Peak Rail cafe, Tim and I set to work on wire brushing and red oxide painting of a number of air intake manifolds destined for the ex-50008 power unit. Chris Bodell's nascent music career meant he was playing a gig in Bakewell on Saturday night so he went home to practice and took his leave of us. Tim was diagrammed for transporting teenagers to a roller disco in Peterborough that evening and so, despite building up some momentum on the inlet manifolds, we reluctantly packed up and I drove us the 100 or so miles back to Peterborough, where the teenagers were transported and Tim and I undertook a mutual debriefing session in The Moorhen at Hampton Vale (Tim's local). Sunday was spent doing more work on the soon-to-be-launched new RRRG website (of which more in due course) and I then hit the road for the final time back to Reading, which was covered in a personal best time of 1 hour 50 minutes and brought my mileage for the weekend to a touch short of 400. But it's all good fun (allegedly!).

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Recovering parts acquired from Rodney Group

A large amount of heavy boulders blocking the path to the container where our purchased spares were.

On Friday 29th June 2012, Sarah and myself set off together with our trusty hound Toby to meet up with the contacted transport company at a site near Worcester to collect electrical items we had purchased from 50021 Rodney Group, this also included a Radiator Fan Motor and Traction Motor Blower for the D400 Fund.

When we arrived at site, we introduced ourselves to the Lorry Driver Nigel Chapman. The first problem we encountered was that due to the heavy deluge the day before, a delivery of large boulders had been delivered and dumped in front of the grounded curtain-sided truck body that our items were being stored in.

After a little head scratching it was decided we could get into the other side of the body if we removed the site security fencing. When we obtained access to the other side of body, the next obstacle was to release the tensioning mechanism, which through the passage of time had sunk into the ground, and after some digging with spades and persuasion with the site dumper truck which lifted the sunk body out of the ground we gained access.

We moved some fencing to gain access to the other side of the container.

With the transport lorry manoeuvred into position and stabiliser legs down the next problem encountered was a temperamental hydraulic hi-ab which with the technical know-how of Nigel, eventually played ball. The first two items strapped up and lifted out were the Cubicle and Rad Fan Motor. The two compressors and traction motor followed soon after. The items were secured down and we then drove to where the traction motor blowers and spare power unit (ex-50045) were stored. One blower motor was lifted and secured down.

We needed the site dumper truck to force our way in...


RRRG's main purchase, the electrical cubicle, safely loaded onto the lorry.

Once everything was checked to be secure we set off on our journey North, up the M5, M42 etc heading for Derbyshire with Bowers Electrical being our first port of call. We had anticipated the journey to be difficult with the usual Friday afternoon traffic, however also had the added problem of road closures along the A6 between Derby and Rowsley due to the Olympic Torch relay, fortunately the journey went without delay or incident. At Bowers we had the assistance of a forklift and very quickly off-loaded D400 Fund's Rad Fan Motor and Blower Motor together with our two compressors.

RRRG's haul included two genuine Class 50 compressors, ex-50011, seen being guided onto the lorry.


We then set off for Rowsley, arriving at site about 4:45pm, where we were met by local “BG” resident Dave Rolfe. Once on site we discovered one of our ETH generators (in worse condition than the others, which is why it was never sent for overhaul) was obstructing the route of the lorry to our storage shed, incidentally we also needed this moving, so with the Hi-ab on site we took advantage and relocated it dropping it near Renown together with the Traction Motor.

A further spare traction motor was also included in the deal.


A short break was had whilst we retired to the BG for a brew. Once refreshed we returned to our storage shed to off-load the electrical cubicle although this was not without problems as the hi-ab could not manoeuvre the cubicle all the way into the shed so with a solid steel bar and some brute force we pushed the cubicle in. Space in the shed being what it was, we had to man-handle the cubicle in at an angle until the doors could be closed and locked.  Everything was then sheeted up, secured and we eventually left for site calling at Frankie & Bennies for a very well earned bite to eat and pint, eventually getting back home some 15 hours after starting out earlier that morning.

After some manhandling to make it fit the available space inside RRRG's designated facility, the newly-purchased cubicle was safely stored awaiting future work. With this final act, a long and satisfying day finally came to an end!

A big thank you to Nigel Chapman the jovial lorry driver, who was a tremendous help on the day, enjoy your retirement!!  Photos by Sarah McCall.

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