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Restoration diary

As one of RRRG's electrical officers I will write about my specialist field as well as general reports of work on site.

Work party report 15th May 2022

Work party report 15th May 2022
Mark Burrows, Jay Hirst and I were on site today.Mark carried on painting air filter frames, while Jay and I continued belling out cables in the electrical cubicle.Ian the welder had been on site last week, and had fitted new grip strips to the engine room and generator compartment floors where Mark had cut out the corroded sections, as seen in my ...
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Work party report 18th April 2022

Work party report 18th April 2022
50030 no 2 cab underfloor heater before refurbishment. Photo by Jay Hirst.
The repaired AWS sunflower in 50030 no 1 end cab. Photo by Jay Hirst.
​Dave Rolfe, Jay Hirst and I were on site today.Dave had removed the stuck covers on the underfloor cab heaters in both cabs, so Jay and I hoovered them out, checked the heating elements were still good, and belled out the wiring to the switch panel above the driver's positions.We replaced the broken base of the AWS button in No.1 cab and I connect...
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Work party report 20th March 2022

Mark Burrows, Dave Rolfe, Carl and Sofy Looker and myself were on site today.Mark finished removing the rust from the engine compartment floor in Repulse where he'd previously cut out the rotten floor treads, generating a Sahara-size dust cloud!. Carl drilled out a rusted floor screw in No.2 cab so I could examine the underfloor heater an...
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Work party report 6th March 2022

Work party report 6th March 2022
Mark Burrows, Jay Hirst and I were on site today working on 50030. Mark cut out the last of the rotten floor treads in the engine compartment ready for Ian the welder to fit new treads, while Jay and I belled out and marked the wiring that goes to the switch panels above the driver in both cabs. Photos in this report courtesy Jay Hirst.
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Work party report 9 January 2022

Jay, Mark and me were on site today. Mark barred the power unit intended for use in 50030 round three and a half times, added more oil and pumped it round. He also oiled the turbos we are storing for later use on this power unit again.Jay and I carried on belling out wiring in the electrical cubicle, finding as we went, some cables where the writte...
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Work party report 14th November 2021

​Mark, Dave, Jay and I were on site today.Mark ground off the remains of the anti-slip treads in the gen compartment where they had rotted away or been broken off, in preparation for Ian the welder to fit new ones. He will also fit new ones in places alongside the engine walkways.Jay and I carried belling out wiring in the electrical cubicle, ...
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Work party report 8th August 2021

Dave Rolfe, Jay Hirst and I were on site. We continued the repetitive and rather dull-but-necessary task of cleaning out the engine room in 50030 ready for the return of the power unit nad overhauled generator in due course.Dave had found some heavy duty degreaser spray, and we used it on the sides of the engine compartment at the generator end whi...
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Work party report 20th June 2021

Work party report 20th June 2021
Carl and Sofy Looker, Dave Rolfe and I were on site on Sunday 20 June and between us we carried on scraping, cleaning and painting the engine room inside 50030, getting to about three quarters prepared and undercoated.
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Work party report 16th May 2021

Work party report 16th May 2021
​Mark Burrows and his son Robert, Jay Hirst and I were on site on May 16th. Following on from the work done by Ian Williams that we talked about previously, we carried on repairing the bodyshell of 50030 taking the opportunity of better internal access whilst the power unit is out. Mark and Robert continued on the outside of the no 1 cab around the...
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Work party report 18th April 2021

Work party report 18th April 2021
A key priority for us now that the power unit is out of 50030 is to get the bodyshell watertight. There's no point us putting overhauled mechanicals and electrical machines back in there if they are only going to get wet! The same applies to the cabs as we move on to refitting and restoring the controls and air pipes behind the driver's desk. We've...
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Work party report 27th October 2019

Carl and Sofy Looker joined me today on site. They started scraping loose paint off the inside of the engine compartment, then washing areas with White Spirit and very soapy water, to see which shifted the accumulated oil film and carbon soot better. The best combination seemed to be White Sprit first, followed by the soapy water. They washed off t...
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Work party report 20th October 2019

Wes Needle, Mark Burrows, Robert Burrows (Mark's son) and I were on site today. Wes carried on sorting 50030 No.1 cab desk panels to make them fit properly, including fitting new hinges, Mark and Robert painted yellow gloss over the new steel on the cabsides and No.1 cab front, to protect them over the winter. I painted the fire extinguisher tubes ...
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Work party report 20th July 2019

I went up again today as welder Ian needed access inside Repulse. Ian Kemp and Peter Carter were also there barring the ex-50008 power unit round and pumping oil through it. We do this as a mattter of course at each work party just to ensure this power unit remains in good internal condition ready for insertion into 50030 later this ye...
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Work party report 14th July 2019

This weekend we had Ian Williams the welder on site, starting the bodywork repairs on Repulse. Joining me today was Mark Burrows, Carl and Sofy Looker.Ian cut out rotten steel around No.1 cab end and along the 'non-visible' side, where we had identified the worst corrosion. He did most of the cutting out yesterday, today was clearing the rusty debr...
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Work party report 6th May 2019

Ian Kemp decided to go to site today as it was a bank holiday and he wasn't working. Wes Needle was available too so I went as well.Quite a productive day, Wes was in No.1 cab again, fitted the windscreen washer control and washer button he'd overhauled, and made a repair to a conduit under the floor. He took away a section of cab panelling to rep...
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Work party report 21st April 2019

Work party report 21st April 2019
I went up to site yesterday as Ian Kemp was bringing some helicoils as a possible solution to the radiator resistor backplate problem (see previous work party reports). After we'd looked at them and decided they may well solve the problem, Ian and Peter Carter took measurements off the power unit for the upcoming lift, barred the engine round as th...
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Work party report 10 March 2019

No 1 end cab 50030 with panelling refitted.
Bogie brake adjusters refurbished and ready for refitting to the bogies to replace worn adjusters removed previously.
A good day on Sunday, despite the Arctic wind in the morning. Wes Needle had a very productive day. He started the day by cleaning the debris from under No.1 cab floor on the second man's side. Then, with Dave's help, they checked the operation of the handbrake mechanism under the floor. They found that the pivot nut required tightening and a new s...
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Work party report 17th February 2019

Dave Rolfe, Wes Needle and I were on site on Sunday 17th February. Peak Rail have been reorganising their site during the first weeks of 2019 and opportunities for work parties were also limited by the weather. Dave was removing the brake adjustment parts off the bogies, as he'd identified some that were either worn or where there appeared to be ...
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Work party reports update December 2018

Ian Kemp, Peter Carter and Dave Rolfe have been finishing off fitting pipework onto the ex-50008 power unit, and have started removing the injectors for inspection, before they go off for overhaul. Dave has been overhauling, cleaning and temporarily fitting items onto the brake frame so we know where everything goes. They will need removing to get ...
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Work party reports July/August 2018

The radiator compartment in 50030 following reinstallation of the overhauled radiators.
Deborah Stokes testing the voltage on the batteries still inside 50030.
The first two radiator fan resistor backplates were refitted on a test basis.
Deborah Stokes removed the batteries from 50030 to top up distilled water levels and attempt to charge them up.
The heat exchanger for the overhauled power unit intended for 50030 was overhauled last year and has now been fully installed complete with all pipework.
After four hours connected to a car battery charger, the voltage on the batteries doubled, although they won't be good enough to actually fire 50030 up.
I have been offline with PC problems for the last few weeks so work party reports haven't been added! So here's a bumper update rolling up all the work on site during the last month or so since the last report in mid July.The last three workparties saw myself, Dave Rolfe, Deborah Stokes, Wes Needle, Carl and Sofy Looker and Mark a...
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